home register FAQ memberlist calendar

Go Back   Turbobricks Forums > Mechanical > performance & modifications

Thread Tools Display Modes
Old 09-07-2019, 01:39 PM   #1
unbalanced chemical
thelostartof's Avatar
Join Date: Jun 2002
Location: Apache Junction, AZ
Default Lower than Expected boost External WG

My 744 has a Tial MV-S that I have been running for 6+ years, unit was new when installed and has been flawless eversince I put it on. I am running a Greddy Profec B Spec EBC that has also been flawless for even longer.

So as of last week all of a sudden my peak boost dropped for each setting, the EBC has High, Low and off which give me 3 boost settings. The Off settings which went off WG spring was running around 11psi and is now at 8psi, low was 16psi and is now 13psi, High was 26psi and is now 21psi. This issue came on very sudden, I was out on a tuning drive to get more e85 and things were going great at 26psi until about 20 min into the drive when i left a stoplight and noticed that the boost was all of a sudden lower and the power just wasnt there.

I have swapped out the Greddy unit for another known working unit along with a combination of control unit and soleniod and both units produce the same results of boost.

I have pressure tested the car pre-turbo to 30psi and found no boost leaks, none of the WG hoses or lines leak, nothing at the intake manifold or any place else. So because of this I am fairly sure that there are no boost leaks.

That leaves me to think the issue has to be the WG, being that the External unit Dumps to atomosphere everything sounds 100% normal, the peak boost is just lower.

So any idea's of what I should check next? This engine has around 1500 miles on it since I rebuilt it and otherwise everything has been perfect including boost control up until last week when all of a sudden I lost a bit of power and boost.

Thank you for the time to read and any help you can offer, the car has been running great and I wanted to finally take it back to the strip to finally go for proper 11's on MS but with this boost control issue it makes it harder to tune without boost being where it should be.

Chip Feedback Thread / PM LH 2.4 Chip Prices
thelostartof is offline   Reply With Quote
Old 09-07-2019, 03:02 PM   #2
Board Member
Join Date: Jun 2003
Location: PDX

check the fire ring on the bottom of the gate, check the valve itself to make sure it isnt sticking partially open, swap in a known good spring.
RvolvoR is offline   Reply With Quote
Old 09-07-2019, 04:31 PM   #3
Board Member
Join Date: Nov 2002
Location: Northern Washington

Mike measure pressure required to get the WG off of it's seat.

May be related to the spring.

If boost threshold is same as before the WG is not leaking badly.
Overkill is consistently more fun.
JohnLane is offline   Reply With Quote
Old 09-07-2019, 07:42 PM   #4
Stiggy Pop
Board Member
Stiggy Pop's Avatar
Join Date: Feb 2011
Location: Granville, MA

I tested my gate with an air compressor, regulator, manual boost control and apparently every adapter fitting I could find in the tool box

'79 242
943 pickup
Stiggy Pop is offline   Reply With Quote
Old 09-08-2019, 12:04 AM   #5
Vintage anti-ricer
gsellstr's Avatar
Join Date: Oct 2004
Location: Somewhere in a northern California smog bank

I know this will sound stupid, but voice of experience here and from Doug as well. Are you sure your gauge didn't go haywire?
Doug Williams "Mr. Doug" 4/15/2009
Pete Fluitman "fivehundred" 7/14/2013
Mick Starkey "TrickMick" 1/10/14
Mark Baldwin "blue850t5" 7/19/18
Nick Fengler "fengler" 8/6/18
Thomas Fritz "stealthfti" 10/11/18

74 144 B20

90 745Ti

If you need Superpro bushings PM me for price and availability!
gsellstr is offline   Reply With Quote
Old 09-08-2019, 01:07 AM   #6
unbalanced chemical
thelostartof's Avatar
Join Date: Jun 2002
Location: Apache Junction, AZ

Boost guage is not just reading low, the lack of the extra 5psi on that holset is very very noticable (something like 50+whp), nevermind that the dash guage also shows the drop in boost. Oh I should mention that the MS datalog also shows the lack of boost also. This is how I validated when it went wrong on the test drive as I happened to be datalogging at the time.
thelostartof is offline   Reply With Quote
Old 09-08-2019, 10:25 AM   #7
F*ck 12
VB242's Avatar
Join Date: Sep 2011
Location: In my 15x20 Corona cell

Exhaust leak at the manifold-head?
"i will destroy all of you!"
-Sheldon Plankton

Booty Scooty
VB242 is online now   Reply With Quote
Old 09-08-2019, 02:01 PM   #8
Comes with a free Frogurt
Duder's Avatar
Join Date: Dec 2009
Location: Torrance, CA

Check your turbine wheel & compressor wheel for damage...
Duder is offline   Reply With Quote
Old 09-09-2019, 07:41 AM   #9
Board Member
Join Date: Apr 2017

If it does the same thing with multiple gates I would suspect a boost leak or exhaust leak causing the turbo to not build boost like it should.
klork is offline   Reply With Quote

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is On

Forum Jump

All times are GMT -4. The time now is 07:40 PM.

Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2020, vBulletin Solutions Inc.