pat244ti
Moderator
- Joined
- Dec 23, 2002
- Location
- Santa Cruz CA
I started a thread in the project forum for this a while ago but I have not been updating it, just been working away and have not had time.
I've been working on converting my 244 race car shell [I gave up on running SCCA with it because of cost] to LeMons spec since about September when I started with this
I sold off pretty much all of the engine go fast drivetrain parts that were on it to fund finishing it safety wise and other general prep mostly.
It's a squirter block with LH 2.2 and breakerless 240 Turbo ignition, stock manifolds, 15g from a 850 Turbo and other stuff.
It was a crazy few weeks leading up to the race, we even started 2 hours after the green because we were waiting on tires [the hoosiers I had on my wheels before were not legal]. Did not run a transponder so we were never being scored.
Had a few mishaps. A connector came loose at the coil for the RPM signal going to LH and caused it to stall/no start, quick fix. When Ben got towed in the airdam got taco'ed by the tow strap hooked to us [never installed a 242GT front tow hook]
A short time later after a driver change, Rob gets pushed in and a wheel comes off while getting pushed by the truck. Minor 1/4 [panel damage], 5 missing lugnuts and ovaled out stud holes on the wheel was the result.
We began coming in every few laps to retighten the lugs.
Sunday morning we did some work, Ben went out first again and missed a yellow flag coming into a hairpin, lost it and creamed the 244's left rear quarter into a GTI that had slowed for the caution. Luckily it was all cosmetic but it was still pretty agonizing to see. The rear 1/4 is destroyed but I will get it replaced, we still did not execute our theme for this race [decorating it like the Daytona USA car "Hornet"] so keeping the silver paint nice [a HS graduation gift from 2003] is officially out of the question.
For the most part Sunday went pretty good other than that. We had to get towed in once for a stuck throttle going up the hill which Rob thankfully nailed the kill switch in time before something bad could happen. We stayed on the track just about all day. Towards the end of the day the car started to run a little funky but it made it past the checkered.
The car ran pretty good, seems a little rich [running s70 t5 injectors] but I am going to dial that out with the maf screw and possibly smaller injectors and or a 2.5 bar fpr. Wideband is almost installed so I will have a better idea of whats going on. The brake lines need to be replaced on all four corners I think they are mad for sitting for so long with an open system, the car will stop fine but the pedal is spongy.
With those items fixed the car should be pretty awesome. Seemed reliable and was fast and handled great in my opinion.
I'll post more pictures later
I've been working on converting my 244 race car shell [I gave up on running SCCA with it because of cost] to LeMons spec since about September when I started with this
I sold off pretty much all of the engine go fast drivetrain parts that were on it to fund finishing it safety wise and other general prep mostly.
It's a squirter block with LH 2.2 and breakerless 240 Turbo ignition, stock manifolds, 15g from a 850 Turbo and other stuff.
It was a crazy few weeks leading up to the race, we even started 2 hours after the green because we were waiting on tires [the hoosiers I had on my wheels before were not legal]. Did not run a transponder so we were never being scored.
Had a few mishaps. A connector came loose at the coil for the RPM signal going to LH and caused it to stall/no start, quick fix. When Ben got towed in the airdam got taco'ed by the tow strap hooked to us [never installed a 242GT front tow hook]
A short time later after a driver change, Rob gets pushed in and a wheel comes off while getting pushed by the truck. Minor 1/4 [panel damage], 5 missing lugnuts and ovaled out stud holes on the wheel was the result.
We began coming in every few laps to retighten the lugs.
Sunday morning we did some work, Ben went out first again and missed a yellow flag coming into a hairpin, lost it and creamed the 244's left rear quarter into a GTI that had slowed for the caution. Luckily it was all cosmetic but it was still pretty agonizing to see. The rear 1/4 is destroyed but I will get it replaced, we still did not execute our theme for this race [decorating it like the Daytona USA car "Hornet"] so keeping the silver paint nice [a HS graduation gift from 2003] is officially out of the question.
For the most part Sunday went pretty good other than that. We had to get towed in once for a stuck throttle going up the hill which Rob thankfully nailed the kill switch in time before something bad could happen. We stayed on the track just about all day. Towards the end of the day the car started to run a little funky but it made it past the checkered.
The car ran pretty good, seems a little rich [running s70 t5 injectors] but I am going to dial that out with the maf screw and possibly smaller injectors and or a 2.5 bar fpr. Wideband is almost installed so I will have a better idea of whats going on. The brake lines need to be replaced on all four corners I think they are mad for sitting for so long with an open system, the car will stop fine but the pedal is spongy.
With those items fixed the car should be pretty awesome. Seemed reliable and was fast and handled great in my opinion.
I'll post more pictures later